The measure phase of the project, as agreed by the team, included the following.
Process mapping:
We conducted a map of the process that was causing us the most issues on the line, the plasma station and the hub attach station. This tool proved to be a very important tool for us when dealing with the kink issue on the line. While monitoring the plasma station we found that a piece of balloon tubing which was put on at the previous station to help prevent kinks on the end of the unit was actually causing the units to kink. The Product Builder at the plasma station puts the units into a hoop to carry the units to the plasma station. While putting the units into the hoop the balloon tubing was getting pushed and logged into the hoop by the Product Builder. When the next unit was pushed into the hoop it was getting caught on the tubing and kinking the unit. The product builder told us that they see this from time to time, but this was never reported to us before this. We were able to inform the product builder at that stage to ensure that they check the hoops before putting units into them and to discard the hoops that had tubing stuck in them. We found 25 out of 50 with balloon tubing in the hoops at the time of the observation.
When we looked at the hub attach station we found that after Hub attach the units are removed from the hoops and placed on a rack to hang. Unless the units are removed carefully there is a potential to kink the unit. A unit was kinked during our observation of this step in the process. We also found that there is also the potential for kinking units when the balloon tubing, which is inserted on to the units at mandrel removal, needs to be replaced back on the unit before removing the full lot to the next station. Below is a Map of the Hub Attach process. This tool is very visual but can be time consuming when mapping out on Mini tab.
We then looked at the biggest issue with that station which was the glue issues with the 2 different types of mandrels. Neither of the mandrels we were using was going to improve our gluing process so we decided that we would look at alternative mandrels and trial these mandrels on what we call shorties. This trial is in process at this time.
Data Collection
For data collection we opted for a p Chart. The reason we opted for this tool was we felt that it had the best visual indicator. These charts enables the user to pull out each scrap reason code and it allows the user to see if the process is out of control with that particular scrap issue See below p chart for 8 lots of IDE units showing the kink issue on the line
Rolled throughput Yield
We now knew what issues were causing the biggest issues on the line but we also wanted to see how the overall line was performing and to do this we took a snap shot of both IDE units and CE units to see how the yield was performing on both types of products. Below is a snap shot of the CE units and the rolled throughput yield for that product.
CE Snap shot of 240 units (RTY)
Station Yield
Station 1 100%
Station 2 99.2%
Station 3 99.12%
Station 4 100%
Station 5 94.5%
Station 6 23.7%